MGF
Head Gasket Failure.
Root
Cause Analysis, Solution Proposal and Validation.
Introduction.
Head Gasket Failure in the MGF is the main concern for owners and
prospective buyers. Most MGF’s seem to suffer at least one failure, and often,
more than that.
Head Gasket Failure is not limited the MGF. All K-Series engines,
including the KV6 suffer – but none as bad as the rear engine MGF.
To understand the root cause of the failure we should look to the design
of the cooling system, we should also think about what features are unique to
the F, and any commonality in the individual failures.
Firstly I will review the system, and instrument the vehicle as
necessary to determine the exact behaviour of the system.
The MGF Cooling System:
1. When cold, the coolant cycles around as shown in Figure(1). I.e. The
radiator is excluded from the circuit.
2. As the coolant flowing in this ‘bypass’ approaches normal operating
temperature the thermostat begins to open.
3. Coolant in the radiator circuit is now able to flow – the coolant
flows across through the open thermostat and into the engine. Figure(2).
4. The thermostat opens and closes accordingly to regulate coolant
temperature by regulating the flow through the radiator circuit.
Fig(1): System flow diagram
before thermostat opens:

(Ignore the narrow pipe running from the
jiggle valve to the header tank, and the narrow pipe running from the cylinder
head to the header tank – these merely allow air bubbles to disperse and
maintain coolant level respectively. They are not involved in the flow)
Fig(2): System flow diagram
after thermostat opens:
Fig(2.)
At this point, it should be noted that the configuration of the K-Series
cooling system is unusual. Normally the thermostat would be located on the
‘outward’ flowing side of the block. It should also be considered, that the
volume of cold water in the radiator circuit is far greater than a front engine
vehicle.
Consider the effect of locating the thermostat here, coupled with the
high volume of water in the system.
HGF
Failure Root Cause Theory.
All of these factors are
easily accounted for in the theory.
Due to the location of the
thermostat, cold coolant is allowed to surge into the block without being mixed
with hot coolant first. The thermostat closes and the cycle repeats.
The significant difference
here is caused by the location of the thermostat. Compared to conventional
engines (e.g. Rover T-Series or O-Series) with the thermostat Located on the
outward side of the engine, the cold coolant mixes with the hot bypass coolant
before entering the block.
There are two further
negative effects caused by the thermostat location.
Proving the root cause theory.
I instrumented my
MGF with a Dewetron 3000 Series
digital/analogue data logger. 4 thermocouples and a GPS receiver. The following
information was logged:
1. Coolant temperature at
the thermostat housing – i.e. cooling inlet temperature.
2. Coolant temperature at
the outlet elbow.
3. Coolant temperature in
the radiator.
5. Engine bay temperature.
6. GPS position – to derive
vehicle speed.
All experiments were
conducted with an outdoor ambient air temperature of +3oC in late December /
early January.


The left hand side of the
unit consists of 8 + 256 analogue inputs. The four pairs of connections on this
panel link to the remotely mounted thermocouple amplifiers. The logger is sat on
top of a 200AmpHr YUASA battery to ensure reliable long term logging.

Results.
The vehicle was started cold
(left overnight).
The run starts with some
mild town driving, a blast up the motorway, followed by a long run through the
countryside. 1hr in total.

A large differential between
inlet temperature and outlet temperature is clear. It is also not a stable
differential.

The
red line shows the difference in temperature between the inlet and outlet side
of the block. The initial climb is expected, but the continual erratic
variation that continues will lead to the predicted thermo-mechanical stress.
The spike at 500seconds corresponds to a sudden increase in the temperature
differential, similar variations follow.
The
data acquired supports this theory. So now to the solution.
The
solution.
We now know the significant
factors that cause the failure:
These two factors must be
eliminated:
So, the objective is the
relocation of the thermostat and reduction in the volume of cold coolant. N.b.
This is not a reduction in the volume of coolant, merely are reduction in the
volume that is not warmed during the warm up cycle in Fig1 above.
The third (and important!)
factor – the modification should be affordable.

Relocating the thermostat as above has the following effects:
·
Reduction of cold coolant in the system. Only the
coolant actually in the radiator is not warmed up gradually during the warm up
cycle.
·
Cold coolant in the radiator is mixed with warm
coolant in the pipe work before it reaches the block.
According to the theory, the
thermal shock caused by temperature transients across the cylinder head is now
minimised, and so the thermo-mechanical shock is also minimised. The setup
should now be much less prone to HGF.
Practical
Application of the Theory.



The donor, in this case, was
two Renault Megane 1.4 petrol engines at the local scrap yard.
Of course, this design
leaves a spare ‘bypass’ connection – I used this for a thermocouple to support
later data logging – you can just block this off.
This design also allows for
a smooth laminar flow once the thermostat is open, the bypass tube is fairly
large bore – more than adequate for the bypass during the warm up cycle.
(An
8mm thick hard aluminium ‘gasket’ has been added since this picture – the
o-ring alone didn’t make a perfect seal against the second plastic housing.)
The remote housing is easily
installed on the F – there is even access from above with the plastic trim in
the wheel well removed:

A suitable T Junction for
the bypass circuit was sourced from a scrap Porsche 944, complete with a
suitable length of hose.

From
Above:


The use of two thermostat housings
means a blank ‘washer’ is required to fill the gap between the mounting face of
the housing and the recess for the thermostat it originally held.
The original MGF thermostat
was replaced with a blank in exactly the same way – created by cutting the
centre out of a scrap thermostat:
Choice of Thermostat.
The normal MGF Thermostat is
set at 88oC. The new location of the thermostat must be accounted for when
deciding what thermostat to use.
To regulate the engine at
the same temperature, the temperature drop along the pipe to the new location
must be taken into account – this was measured as about 10oC in the previous
experiment.
A Rover 620Ti thermostat –
set at 78oC is ideal. The T-Series thermostat housing requires a ‘valve’ type thermostat,
which closes the bypass when open – the valve plate is easily removed for our
application.
The
results:
The same route was repeated
after the modifications had been made.
The car was left overnight,
to ensure it was completely cold, and the ambient was again about 3oC.

It can be seen immediately
that the temperature differential across the head is now smaller, and the
variations in the differential virtually non existent. The warm up cycle is
smoother, and the thermostat only opens once – this time smoothly. (It is not
forced shut by an inrush of cold coolant).
Comparison
pre/post modification.

The
temperature at the inlet to the cylinder head has less erratic variation and a
smoother warm up cycle.

Outlet
temperature also has less erratic temperature differential.

The
radiator now operates at a higher temperature – variations are again less
erratic. The higher operating temperature reflects the improved performance of
the water pump.

Processing
the data shows the drastic improvement in head temperature differential. The
key here is that the blue line (post modification) is lower and more stable –
the erratic changes in the red line are the root cause of the HGF – the
temperature differential is also 40% greater before the modification.

The
difference is clear – and the warm up time is not noticeable affected.
An
additional test was conducted post modification.

Conclusion.
The modification has had the
desired effect. Without any ill side effects.
The temperature variations
have been minimised and the volume of cold coolant drastically reduced.
The cumulative effect of
repeat stress cycles will eventually lead to a mechanical failure – be that the
wet liner sinking, the bolts stretching or the water pump failing – with this
stress now minimised, HGF should be much less likely.
Extra
Supporting Evidence.
The theory and results above
explain why: the 4mm hole added to the thermostat maintains a continuous flow
even whilst the thermostat is closed. The cold coolant in the system is warmed
up during the warm up cycle. However, the warm up cycle is extended in this
case.
Intuitively you might think
they would be first to go. However, the thermostat is removed on these cars to
reduce restrictions in the coolant flow to allow better cooling when driven
hard – the knock on effect is elimination of the thermal shock experienced by
the cylinder head.
Other
Causes of HGF.
It should be noted, that the
poor coolant system design is not the only cause of HGF in the MGF.
David Monks. Uk 2006.
Credits and Acknowledgments.
This article has not been written
for financial gain!
Credit
is due to the following websites and articles:
‘Overheating
MGF – Don’t Just Assume – Check!’ - Roger Parker, Enjoying MG 2006.
Rob
at http://www.mgf.ultimatemg.com/
Dieter
at http://www.mgfcar.de/
Dave
at http://www.rovercarhospital.co.uk/
Carlos
at http://web.tiscali.it/elise_s1/index.htm